E6581611
M-2
13
(Continued)
Error code Failure code Problem Possible causes Remedies
000B Overvoltage during
deceleration
The deceleration time is too short.
(Regenerative energy is too large.)
Increase the deceleration time .
Overvoltage limit operation is set
to 1. (Disabled).
Set overvoltage limit operation to
0, 2, 3.
The input voltage fluctuates abnormally.
(1) The power supply has a capacity of
500kVA or more.
(2) A power factor improvement capacitor is
opened and closed.
(3) A system using a thyristor is connected
to the same power distribution line.
Insert a suitable input reactor.
000C Overvoltage during
constant-speed
operation
The input voltage fluctuates abnormally.
(1) The power supply has a capacity of
500kVA or more.
(2) A power factor improvement capacitor is
opened or closed.
(3) A system using a thyrister is connected
to the same power distribution line.
Insert a suitable input reactor.
The motor is in a regenerative state
because the load causes the motor to run
at a frequency higher than the inverter
output frequency.
Install an optional dynamic braking
resistor. (optional)
000D Inverter overload
The acceleration time ACC is too short. Increase the acceleration time .
The DC braking amount is too large. Reduce the DC braking amount
and the DC braking time .
The V/F setting is improper. Check the V/F parameter setting.
A restart signal is input to the rotating
motor after a momentary stop, etc.
Use (auto-restart) and
(ride-through control).
The load is too large. Use an inverter with a larger rating.
000E Motor overload
The V/F setting is improper. Check the V/F parameter setting.
The motor is locked up. Check the load (operated machine).
Low-speed operation is performed
continuously.
An excessive load is applied to the motor
during operation.
Adjust to the overload that the
motor can withstand during operation in a
low speed range.
003E Main module
overload
The carrier frequency is high and load
current has increased at low speeds
(mainly at 15Hz or less).
Raise the operation frequency.
Reduce the load.
Reduce the carrier frequency.
When an operating motor is started up at
0Hz, use the auto-restart function.
Set carrier frequency control mode
selection f316 to 1 (carrier frequency
with automatic reduction).
000F Dynamic braking
resistor overload trip
The deceleration time is too short.
Dynamic braking is too large.
Increase the deceleration time .
Increase the capacity of dynamic braking
resistor (wattage) and adjust PBR
capacity parameter .
*
0020 Over-torque trip 1
Over-torque reaches to a detection level
during operation.
Enable (over-torque trip selection).
Check system error.
0041 Over-torque trip 2
Output current reached f601 or more
and maintain in f452 during power
running.
Power running torque reached f441 or
more and maintain in f452 during
power running.
Reduce the load.
Increase the stall prevention level or
power running torque limit level.
* This marking trips can be selected valid or invalid by parameters.
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